石油化工设备技术 ›› 2025, Vol. 46 ›› Issue (6): 10-14.doi: 10.3969/j.issn.1006-8805.2025.06.003

• 特约稿件 • 上一篇    下一篇

蒸汽透平调速器错油门工作异常造成转速波动问题研究及对策

刘国帅,邱宏斌,何承厚   

  1. 中国石油化工股份有限公司化工事业部,北京 100728
  • 收稿日期:2022-12-16 修回日期:2025-09-10 接受日期:2025-10-28 出版日期:2025-11-19 发布日期:2025-11-19
  • 作者简介:刘国帅,男,2004年毕业于河北科技大学化机专业,工学学士,长期从事设备管理工作,现任中国石化化工事业部设备室高级主管,高级工程师,已发表论文3篇。
  • 基金资助:
    中国石油化工股份有限公司(批准号:323120;合同编号:30650000-23-ZC0607-0011)资助的课题

Research on Rotation Speed Fluctuation Caused by Abnormal Operation of Steam Turbine Governor Pilot Valve and Countermeasures

Liu Guoshuai, Qiu Hongbin, He Chenghou   

  1. Chemical Department of China Petroleum & Chemical Corporation, Beijing, 100728
  • Received:2022-12-16 Revised:2025-09-10 Accepted:2025-10-28 Online:2025-11-19 Published:2025-11-19

摘要: 在乙烯原料重质化、多样化形势下,研究裂解气压缩机等重要设备操作及运行问题,破解设备运行瓶颈,对实现乙烯装置长周期运行有着重要意义。压缩机与蒸汽透平通过“驱动-被驱动”方式构成机械耦合关系,蒸汽透平作为动力源,与作为负载的压缩机共同组成“动力-负载” 系统,其协同运行状态是否稳定是决定工艺装置安全性与经济性的关键因素。蒸汽透平的转速波动将直接传递至压缩机,进而引发工艺参数紊乱、设备机械损伤、能耗上升等问题,对装置的运行稳定性和安全性构成显著威胁。文章对某乙烯装置裂解气压缩机蒸汽透平大修后出现转速波动的情况进行了介绍,并结合异常现象对导致该问题的原因进行了分析,通过采取各项措施逐一进行排查,最终确定故障部位为错油门。对错油门的结构和运转机理进行深入研究发现导致故障的原因是错油门内的润滑油流动状态不良,致使滑阀内产生油焦,进而引起卡涩。通过调整错油门卸油孔调节阀增大喷油量,解决了该问题。

关键词: 错油门, 透平, 转速, 波动

Abstract: Under the current trend of heavier and more diverse ethylene feedstock, it is of great significance to study the operation and performance of critical equipment such as cracking gas compressors and addressing operational bottlenecks for achieving long-term stable operation of ethylene plants. The compressor and steam turbine form a mechanical coupling relationship through the "driving-driven" mechanism. As the power source, the steam turbine together with the compressor, acting as the load, constitutes a "power-load" system. Their coordinated and stable operational state is a key factor determining the safety and economic efficiency of the process unit. Fluctuations in the steam turbine's rotation speed are directly transmitted to the compressor, leading to issues such as process parameter instability, mechanical damage to equipment and increased energy consumption. This poses significant threats to the operational stability and safety of the unit. This paper addressed the issue of rotation speed fluctuations observed in the steam turbine of a cracking gas compressor at an ethylene plant following a major overhaul. It analyzes the causes of the problem based on the abnormal phenomena, detailed the step-by-step troubleshooting process involving various corrective measures and ultimately identified the governor pilot valve as the root cause of the failure. Through in-depth research on the structure and operational mechanism of the pilot valve, it was discovered that poor lubricant flow conditions within the throttle valve led to oil fouling and sticking of the sliding valve. By adjusting the oil discharge hole regulating valve of the pilot valve and increasing the oil injection volume, the problem was resolved.

Key words: pilot valve, turbine, rotation speed, fluctuation