石油化工设备技术 ›› 2020, Vol. 41 ›› Issue (5): 53-58.doi: 10.3969/j.issn.1006-8805.2020.05.011

• 检维修技术 • 上一篇    下一篇

乙烯装置低温甲烷泵机械密封失效原因

古红星,周琳,周家成,王小严,赵攀   

  1. 中国石油独山子石化公司乙烯厂乙烯一联合车间,新疆 独山子 833699
  • 收稿日期:2020-04-27 出版日期:2020-09-25 发布日期:2020-09-25
  • 作者简介:古红星,男,2015年毕业于西南石油大学过程装备与控制工程专业,工学学士,主要从事乙烯分离内操工作,助理工程师。Email:1913099562@qq.com

Cause Analysis and Optimization of Seal Failure of Cryogenic Methane Pump in Ethylene Plant

Gu Hongxing, Zhou Lin, Zhou Jiacheng, Wang Xiaoyan, Zhao Pan   

  1. PetroChina Dushanzi Petrochemical Company, Dushanzi, Xinjiang, 833699
  • Received:2020-04-27 Online:2020-09-25 Published:2020-09-25

摘要: 低温甲烷泵是采用深冷分离技术的乙烯生产装置中的重要设备。文章以低温甲烷泵机械密封频繁失效为切入点,阐述了低温甲烷泵的密封机理,并根据密封机理分析判断出引起该泵密封液外漏和内漏的原因有二:一是泵叶轮侧滑动轴承自润滑效果差,不能形成稳定的润滑液膜,导致轴承与轴套存在干摩擦,引起泵的振动,加剧动、静环分离;二是波纹管环面内径承压平衡比过小,动、静环耐压性不足,导致密封腔密封压差过大。根据分析结果采取如下有效措施进行改进,即:制定优化改造方案,对轴承进行重新改造,改善自润滑效果;用截面矩形环面替换原有L型环面,提高密封波纹管内径承压比;使用更耐压的PG型矩形截面密封圈并升级密封圈材质;同时优化机泵运行监控手段,提高机泵运行寿命,减少不必要的检修工作。

关键词: 甲烷泵, 机械密封, 轴承, 密封压差, 承压比失效, 优化

Abstract: Cryogenic methane pump is important equipment in ethylene production plant using cryogenic separation technology. Taking frequent mechanical seal failure of cryogenic methane pump as the starting point, this paper expounds the sealing mechanism of cryogenic methane pump. Itdeterminedfrom the analysis of the sealing mechanism that there were two causes for the leakage of sealing fluid. First was the poor self-lubrication effect of theside sliding bearing of the pump impellerwhich could not form stable lubrication liquid film, resulting in dry friction between the bearing and the shaft sleeve. And this led to the vibration of the pump and intensified the separation of the rotor-stator ring. Second was the smallinner diameter pressureratio of the bellows ring surface and the insufficient pressure resistance of the static and dynamic ring, resulting in big sealing pressure difference of the sealing cavity. According to the analysis results, the optimized transformation scheme was adopted to reconstruct the bearing and improve the self-lubrication effect. The original L-shaped torus was replaced by a rectangular torus with a section to improve the pressure ratio of the inner diameter of the sealed bellows. More pressure-resistant PG rectangular section was used for the seal ring and the seal ring materialwas upgraded. Meanwhile, the pump operation monitoring means was optimized toprolong the pump operating life and reduce unnecessary maintenance work.

Key words: methane pump, mechanical seal, bearing, sealing pressure difference, pressure ratio, failure, optimization